Finally got her back together this arvo.
WOW what an improvement.The low and mid range response is greatly improved,even got the TC to cut in on the dirt in 2nd gear





Hopefully all this regained power will also equate to regained economy.
Over the last 3 weeks she has had the following long overdue work done.
All fluids/filters changed
Drive belt
Glow Plugs
Oil pressure sender
Provent
All cooling system hoses changed
Nanocom/3 amigoes banished
EGR removal kit
Exhaust gasket
Manifold webbing removed and 6 outer holes drilled larger
Wastgate adjusted,more adjusting to try.
Intercooler/radiator cleaned inside and out,AC cleaned.LOTS of caked mud in all 3
Engine Saver.
Im putting the performance gains down to a combination of the following.
Repair of leaking exhaust manifold.
Adjustment of wastegate.
Thorough Cleaning of the 3 radiators.
EGR removal.
An interesting point with the manifold.It WAS warped,around 3mm in total.After cutting the webbing out it was less than 1mm so I didnt bother getting it machined.Removing the webbing definately de-stresses it.I used a 5" grinder with a mega line disc.Just cut wedges out till I couldnt anymore then put on a grinder disc to tidy up.Half an hour including drilling the stud holes bigger on the 6 outside holes.
Off on an overnite camping trip tommorow,hopefully she appreciates all the attention and behaves!!!!
Andrew