Ozdunc
22nd November 2017, 06:26 PM
Howdy chaps, been a while.
After 4 years of running well, old Bill decided to start stuttering on small pedal inputs. If I had thought for a bit I'd have checked the plug leads, but I didn't and I saw that the butterfly spindle on the old Zenith was leaking fuel so I decide to swap out for a new Zenith I've had lying around.
Now I've faced the main joint between the top and bottom of the carby, the O ring is good and in the right position and the float height is correct at 33m.
I've adjusted the tappets, changed the plugs and leads. Timing is around 6deg BTDC and vacuum gauge is rock solid at 20mmHg when warm
Issue is this:
Idles beautifully at around 500, and starts no choke. Pulls hard on full throttle but stumbles low down as it was with the old carby. If I drive with the choke out the low end is great but as you'd expect it it starts to strangle at the 3000+
Volume mixture is out about 3 1/2 turns already. At 1.5 turns out (the recommended starting point) it barely runs. I adjusted the volume screw out until the vacuum gauge stopped fluctuating and it stopped 'chuffing' out the exhaust.
From there I'd do a run, it still hesitates, so I'd add a 1/4 on the volume screw and repeat. I've gone too far and dialed it back a 1/2 but I'm not getting a sweet spot to eliminate this hesitation.
Spraying carby cleaner around the base of the carby doesn't do anything, so I think there's no leaks between the carby and the manifold.
Old plugs were light gray, so I think it had been running a bit lean, but that might also be lots of short journeys.
What am I doing wrong?
After 4 years of running well, old Bill decided to start stuttering on small pedal inputs. If I had thought for a bit I'd have checked the plug leads, but I didn't and I saw that the butterfly spindle on the old Zenith was leaking fuel so I decide to swap out for a new Zenith I've had lying around.
Now I've faced the main joint between the top and bottom of the carby, the O ring is good and in the right position and the float height is correct at 33m.
I've adjusted the tappets, changed the plugs and leads. Timing is around 6deg BTDC and vacuum gauge is rock solid at 20mmHg when warm
Issue is this:
Idles beautifully at around 500, and starts no choke. Pulls hard on full throttle but stumbles low down as it was with the old carby. If I drive with the choke out the low end is great but as you'd expect it it starts to strangle at the 3000+
Volume mixture is out about 3 1/2 turns already. At 1.5 turns out (the recommended starting point) it barely runs. I adjusted the volume screw out until the vacuum gauge stopped fluctuating and it stopped 'chuffing' out the exhaust.
From there I'd do a run, it still hesitates, so I'd add a 1/4 on the volume screw and repeat. I've gone too far and dialed it back a 1/2 but I'm not getting a sweet spot to eliminate this hesitation.
Spraying carby cleaner around the base of the carby doesn't do anything, so I think there's no leaks between the carby and the manifold.
Old plugs were light gray, so I think it had been running a bit lean, but that might also be lots of short journeys.
What am I doing wrong?