View Full Version : Let the fun begin 4bd1 to r380 in defender 130 twin cab.
Bazzle218
3rd December 2020, 08:24 PM
After months of waiting for conversion parts they finally arrived. In the next month or so I will be doing the conversion myself with help from mates. I will post some pictures as it gets done. Unfortunately it will take awhile as i work full time and can only do occasional weekends and an hour or so every other night.
Anyway: Day one 4bd1 engine fitted left hand engine mount bracket to engine using original bolts had to put an extra washer under the head. Fitted aircon bracket from KLR. Easy job hardest part was running a tap through the bolt holes to clean them up. Bloody humid in Townsville .
The next hurdle and i reckon the hardest part of the whole conversion is removing the spigot bush housing to fit the modified one to suit the r380. At this stage we will make a simple puller using 3/4 threaded bar weld nut to housing and using spacer to wind it out. Another method mentioned is drilling the mount putting in a grease nipple and hydraulically push it out using grease. This will be a last resort unless some can confirm there is a recess behind the bracket and crank i dont feel like drilling holes in it. A picture would be good. I have seen the posts in good oil as well. Baz
Bazzle218
7th December 2020, 07:07 PM
The next hurdle and i reckon the hardest part of the whole conversion is removing the spigot bush housing to fit the modified one to suit the r380. At this stage we will make a simple puller using 3/4 threaded bar weld nut to housing and using spacer to wind it out. Another method mentioned is drilling the mount putting in a grease nipple and hydraulically push it out using grease. This will be a last resort unless some can confirm there is a recess behind the bracket and crank i dont feel like drilling holes in it. A picture would be good. I have seen the posts in good oil as well. [/I]
Well as above it took more time to set up welder then remove. 2 x 3/4 zinc nuts, 2 x 3/4 washers, 1 x 24 inch 3/4 zinc booker bar . $13.00 bunnings.
10 mil plate with 3/4 + hole, length of pipe, supplied by mate. One large shifter and bobs your uncle. Crank bolt 41 mm 3/4 socket to stop rotation of crank. After first rotation of nut wound out with little to no pressure. Refitted new spigot carrier and bush tapped it in using the old 4 by 2 as a drift.
Zcoota
15th January 2021, 11:01 PM
How is the conversion going ? Success ?
Tins
15th January 2021, 11:24 PM
https://utreon.com/v/YRDvEhdu41U
It's also on YT but I can't find it atm. Mike does what you are doing.
Bazzle218
23rd January 2021, 07:12 PM
I cracked under the pressure ( had some spare cash) and lashed out on a turbo kit from down south. Just awaiting it to arrive i am guessing March and then will plan 7 days straight for the conversion. My plan is day one remove old radiator including air-con components, motor and everything else. Day two, with box in situ, remove and refit mod bell housing. Offer up 4bd1/t mark up and remove engine weld in engine mounts. Depending on time bolt it all back together engine box. Then 3 days for reassembly and getting various hoses made . I currently have everything to assemble it, nuts bolts washers. Baring any unforeseen issues it should be good go. Biggest issue is its my daily driver so cant have it off road for to long.
Bazzle218
15th May 2021, 06:09 PM
Engine has not been fitted up yet but Turbo Kit arrived from down south. I made the mistake of opening the box . 3 hours later its mounted up. Manifold and turbo mounted, oil feed and return fitted up. cross over pipe and air intake loosely fitted, will remove and hard fit when engine in the bay. Tomorrow modify air filter, Then that's it for a week or so.
1. Instructions supplied clear and concise. All items fit as per supplied.
Exhaust Manifold tips. The bottom nut on number three is fiddley to get on. I followed instructions loosely fitting nuts to allow access to start. Now trying to get a spanner in to tighten it is a nightmare. My solution and it worked a treat, I removed engine cover where engine breather large pipes goes in just above started motor. 2 bolts and a tap off it comes. With this removed i was able to access the nut with a thin open ender and tighten it up. I recon it added 10 minutes to the process. No other real dramas.
The supplier requests that not to much specification information on kit be handed out. I will respect this and not supply any specifications on an open forum. I will update on any handy hints that i discover on my journey. Baz
Bazzle218
2nd June 2021, 07:53 PM
Over the last few evenings approximately 2hrs each night things have progressed.
Radiator, intercooler and aircon components removed. Aircon pipes the biggest pain, p clamps galore. Tag and remove disconnect all wiring and fuel pipes. General preparation for engine removal.
Tonight remove engine, bit of a mission by yourself but do able. Using jack to support gearbox, will sort something out tomorrow.
Friday evening plans are change clutch master cylinder, been weeping for awhile. Then move onto removal of bellhousing and refitting KLR modified one.
Standby for further updates. Baz
Bazzle218
3rd June 2021, 07:27 PM
This evening i removed the r380 bell housing in situ, and did a dry run on fitting the KLR conversion bell housing. It fitted up no worries, well made and tight tolerances.
I have to modify a 18mm or get a stubby spanner to tighten supplied stud access is hard but not doable. (tomorrows job). The original M12s holding the r380 bell housing on appear to have been Loctited and required a gut busting effort to manually remove. My 24v rattle gun which has never let me down did. Of course i cant find my bottle of medium loctite so will get another.
Hint of the day only use single hex sockets. There is far less chance of rounding off the bolts/flange nuts. Since adopting this approach have not rounded of a bolt for years.
Bazzle218
6th June 2021, 03:10 PM
Sunday: with the help of two mates. Motor mated to bell housing without clutch components fitted secured by 4 bolts. Fitted quality engine mount bracket to chassis supplied by Ridji, after bolting them to engine mounts spot welded to chassis. Removed engine leaving chassis mount in situ. My mate (boiler maker)
then welded them in properly . then fitted up clutch plate and bell housing internals. Refitted engine and dropped back in .
Basic tools required. Time from start to finish 4 hours. Don't get excited , plenty of minor stuff to go . Wiring using the 300 tdi wires, cant see an issue. just a pain in the arse. sourcing power steering hoses and plumb it up. As i broke my alternator pully (dont ask) and cant source a second hand one will bite the bullet and buy a new one (alternator) and keep the old one as a spare.
Next job refit clutch master and get a flexible hose made up. It will run under the bell housing secured by p clamps to the slave cylinder i will be fitting a banjo fitting to the slave end for easier fitment, Once thats sorted this week . accelerator cable and stop cable then depending on time fitting alternator/ aircon compressor and sourceing dump pipe or whole exhaust system. [biggrin]
Baz
86mud
8th June 2021, 11:54 AM
Any pictures of the progress?
Bazzle218
8th June 2021, 02:52 PM
Hope this works
Bazzle218
4th July 2021, 05:03 PM
Engine and turbo kit: Conversion straight forward and all supplied items fitted up no issues.
r380 gear box running disco transfer. Engine pulls fine with this gearbox. I find that the engine does not appear to labour, 100kph engine is cruising along and plenty to give if i was to put boot into it.
5th gear: engine has plenty of torque and i can see how people could forget to change down on hills. Small incline which had the 300tdi laboring. the 4bd1 cruises up effortlessly.
I have adjusted fueling as per supplied guide with Turbo Kit . I have no smoke on acceleration or going up the gears. I could wind it out more but will leave well enough alone.
Engine temp: Modified v8 radiator. Sits on about 85 on VDO gauge. Head temp taken from the back of the head reads 70=75.
All things taken into account more then happy. I will be heading up the cape towing a camper trailer at the end of the month so will provide feed back after trip.
If you want to know who I bought the conversion kit off pm me for details.
Last but not least Spanner rating: if you can read a guide and have a mate handy with a welder I rate it about 3 out of 5 spanners to do. Also plenty of advise of forums. Baz
Vern
4th July 2021, 05:25 PM
I'd be guessing here, klr and klr for the 'kits'?
86mud
30th July 2021, 01:32 PM
Good Work Baz. A cape trip will be a great way to bed it in.
Bazzle218
24th August 2021, 05:10 PM
Well back from my trip towing camp trailer and sundries gestimation about 2 tons all up. Happy to report other then a small fuel supply issue which i will get to no issues. Temperature sat on 83c head temp 73. It varied going up some steep ranges but happy to report nothing over 88 with head temp showing max of 80. Dropped back to normal within a minutes of cresting hill. Towing with the r380 with discovery transfer, seamless. 4th gear 95 kph to 100. Occasional run in 5th crept up over 110 kph without effort but i eased up back to 100kph. Fuel economy worked out about 12.5 per 100. Happy with that. Fuel Issue : After sitting for a night it would start and drive about 30 klm and then starve for fuel and stop. It took a bit to work out but it was a bit of me and the original 300 tdi pick up. I run a Brown and Davis long range tank and prior to the trip (a few days) the pickup/sender started to weep. I drained the tank and pulled it out and resealed with fuel safe gasket/silicon NOT. Anyway only way it would bleed up after the stop was to blow back through the fuel lines and it would run fine for the rest of the day. Not a big issue just a pain in the arse. Once home i dropped tank and gave it a good clean out. A few balls of silicone. Anyway i was buggered if i could see any real issue. My mate who was over pointed out that when looking through the pickup pipe there appeared to be a small tag of plastic where the metal pipe was pushed into the black plastic through pipe. It had been there since manufacture . My theory was that the 4bd1 has a different flow rate and when started after the fuel settled it picked up a silicone ball and acted as a flapper valve. Anyway cleaned out the pipe with some effort and a small round file and now no issue. You live and learn. Anyway all good now. Would i do the conversion again yes. Baz
Powered by vBulletin® Version 4.2.4 Copyright © 2026 vBulletin Solutions, Inc. All rights reserved.