prelude
23rd August 2024, 05:34 PM
Hi Lads,
This is a bit of a write up regarding the installation of a 12V A/C compressor so that others may benefit of it, perhaps :)
First, let's answer the "why" question, since our beasts have a proper working A/C to begin with. I decided some time ago that I would like to have the option to run A/C during the night, even if it is only on a ridiculously low setting, just to make it through the worst of conditions. In order to achieve this goal one can go two, maybe three routes:
install a separate system, either 12v or 220v
use one of them portable things
modify the existing system
Mounting an extra system uses up a lot of space and weighs a lot, especially if you go for a domestic split-system since that also requires quite a large and heavy inverter. Those portable things have near useless efficiency and are bulky items difficult to store anywhere and IMHO more of a gimmick. Modifying the existing system brings it's own challenges which I will go into below, it is not for the faint hearted :)
I decided that I did not want to add the extra weight of a separate system and started looking into using the existing climate control system that came from the factory. The easiest way to make that work would be to alter the HEVAC controls so that they can work when stationary (ie. engine not running) and replace the belt driven compressor with an electric unit. After a lot of digging around I found that for 12 volts there are only a few options really; a very ubiquitous 18cc unit and a more rare 20cc variant. Smaller versions also exist like a 14cc and even 12cc but I did not think them adequate for the job. So, I decided to bite the bullet and buy the 18cc version directly from china to cut out the middle man which may or may not have been a good choice... read on :)
In order to make this story about the compressor mostly and not about the HEVAC, which is a story in and of it self, suffice it to say that in the end I will be replacing the current HEVAC controls/computer with an arduino based solution. Effectively I will be building my own climate control that will make use of all the existing sensors, blowers and blend motors. Having said that, to test the compressor and see if it would actually even work I simply plumbed it into the existing system.
Since I will be fabricating a raised air intake for the engine anyway I removed the air box and intake from the engine bay and mounted the MAF sensor directly to the intake plenum and one of those cheap cone shaped "sports" filters directly after it so that I can still drive the car. In this country dust is virtually non existent and sucking in hot under bonnet air is not a problem for the time being. I mounted the electric compressor on the spot where the air box used to live and hooked it up temporarily to see if it would run. Due to a mishap I unfortunately cooked the driver board inside the unit and that is where the first big reason NOT to go electric pops up...
Most, if not all, of the 12v (and higher DC voltages) compressors are pretty much made in the same factory or by the same concept at the very least. The consist of a scroll type compressor driven by a brushless DC motor which in turn is driven by a 3-phase driver. In order to cool the DC motor and the driver board, which is fixed to the aluminium housing with copious amounts of thermal paste, the suction side of the compressor flows through the housing and motor. On top of the driver board sits a controller that knows how the turn the motor in the right direction and provides a soft start by ramping up from 0 to the desired RPM. This controller takes it's input from either a 3 setting lead (4 wires) which allows you to select 2000/3500/5000 rpm or takes a 400h PWM signal where 5% duty cycle is 2000 RPM, 65% duty cycle is 3500 RPM and 95% duty cycle is 5000 RPM. The version you order does not matter since the internal connector is the same and you can simply switch the lead from one to the other. I have not yet tested PWM. In any case, it is the lower driver board that contains a bunch of beefy FET's that failed and I tried to see if I could either repair it, remake another version of get some spares.
Suffice it to say that our chineese friends are not in the habit of producing anything that is even close to durable so spare parts were of course never thought of. You are supposed to consume product and buy more when something breaks. This has put of me off of these units but after some soul searching I had to come to the conclusion that I am already invested in this solution and I had to push on with it. So, I ordered another complete compressor thinking that at least I had a spare one when the mechanicals would wear out.
Now that I had a working compressor I checked my dodgy test wiring at least 5 times to not burn out another unit and.. it started spinning :) Once I had that all set up I mounted a relais between the original compressor clutch power connector and ground and wired the 12v unit up so that it would switch the high setting. After triple testing that everything worked as it should I drove to my local A/C shop to make an appointment for some custom work. Yesterday I finally got to get the entire system plumbed up and it was a good day of working alongside the experts. Really nice blokes who got my idea and simply allowed me to work along side them in their workshop. I did all the "range rover specific" stuff, or should that be "my handywork" :) and they were there to help with the A/C specific stuff. In the end we removed the flexible hoses that run to the original compressor from the aluminium pipes and replaced them with new ones and some angled fittings that were then routed to the new compressor. All in all not that much material was needed to get that done since the original plumbing already routed through that area, but still half a days work.
Then came the BIG moment! filling up the system and checking if it works. Originally the P38 contains 1250 grams of r134. The guy at the shop figured since we altered the plumbing and removed the original compressor which has a large internal volume that we should reduce that to 900 grams and take it from there. I fired up the engine, turned the HEVAC to "LO" and full blast and waited to see what happens. To my relief the "little compressor that could" was capable of running in a system that was designed for a much bigger capacity compressor! The suction line got nice and cold, the air blowing out the vents was freezing and the cycling (because the evaporator would freeze or any other reason the HEVAC computer would toggle the clutch) worked as well, though not as the belt driven unit would behave.
When we tested the system at around 20c we got 2 bar (130 psi) low side and 9 bar (130 psi) high side which is about right. I took the car for a drive with an eye on the current measurements from my victron shunt and I must say, the A/C worked well. Of course we still need to have a 30C + day which we will have next week so that should be interesting. The total current drawn by the vehicle never got much over 110A (and I know the car uses around 30 when just running) but at idle (in drive at the stop lights) the voltage would drop to around 12.5v so clearly the alternator that I currently run is not able to keep up at such low RPM's and the battery cops a beating for a few seconds.
The one thing I did observe is that the ramp-up of the compressor is quite slow and the HEVAC does not understand this, that is to say it is not designed for that. So when the compressor is disengaged, it does not ramp down slowly, it just stops. But when the A/C request line is brought up high again in stead of the evaporator immediately cooling down again it slowly cools down and since the blowers did not slow down you can feel the humidity from the evaporator entering the cabin just briefly. Suffice it to say that my own climate control algorithm will have to take that into account. Perhaps I will simply run the compressor speed up/down as required to keep the evaporator in equilibrium.
What's next? Well I intend to test the pants of the system whilst my car is still in running condition, ie. before I start work on the other projects. Next week is probably the last week of 30+ temperatures in this neck of the woods so I also plan to play around with the A/C then. I will try the low and medium setting and see what that does and see how the entire thing will cope with a heat soaked car that has stood in the sun for quite some time etc. I reckon that it will be able to handle, just, but that is good enough since my build will remove a lot of windows, replacing them with insulated walls so there will be a larger area to cool, just not one that will have that much light incidence.
To be continued :)
Cheers,
-P
This is a bit of a write up regarding the installation of a 12V A/C compressor so that others may benefit of it, perhaps :)
First, let's answer the "why" question, since our beasts have a proper working A/C to begin with. I decided some time ago that I would like to have the option to run A/C during the night, even if it is only on a ridiculously low setting, just to make it through the worst of conditions. In order to achieve this goal one can go two, maybe three routes:
install a separate system, either 12v or 220v
use one of them portable things
modify the existing system
Mounting an extra system uses up a lot of space and weighs a lot, especially if you go for a domestic split-system since that also requires quite a large and heavy inverter. Those portable things have near useless efficiency and are bulky items difficult to store anywhere and IMHO more of a gimmick. Modifying the existing system brings it's own challenges which I will go into below, it is not for the faint hearted :)
I decided that I did not want to add the extra weight of a separate system and started looking into using the existing climate control system that came from the factory. The easiest way to make that work would be to alter the HEVAC controls so that they can work when stationary (ie. engine not running) and replace the belt driven compressor with an electric unit. After a lot of digging around I found that for 12 volts there are only a few options really; a very ubiquitous 18cc unit and a more rare 20cc variant. Smaller versions also exist like a 14cc and even 12cc but I did not think them adequate for the job. So, I decided to bite the bullet and buy the 18cc version directly from china to cut out the middle man which may or may not have been a good choice... read on :)
In order to make this story about the compressor mostly and not about the HEVAC, which is a story in and of it self, suffice it to say that in the end I will be replacing the current HEVAC controls/computer with an arduino based solution. Effectively I will be building my own climate control that will make use of all the existing sensors, blowers and blend motors. Having said that, to test the compressor and see if it would actually even work I simply plumbed it into the existing system.
Since I will be fabricating a raised air intake for the engine anyway I removed the air box and intake from the engine bay and mounted the MAF sensor directly to the intake plenum and one of those cheap cone shaped "sports" filters directly after it so that I can still drive the car. In this country dust is virtually non existent and sucking in hot under bonnet air is not a problem for the time being. I mounted the electric compressor on the spot where the air box used to live and hooked it up temporarily to see if it would run. Due to a mishap I unfortunately cooked the driver board inside the unit and that is where the first big reason NOT to go electric pops up...
Most, if not all, of the 12v (and higher DC voltages) compressors are pretty much made in the same factory or by the same concept at the very least. The consist of a scroll type compressor driven by a brushless DC motor which in turn is driven by a 3-phase driver. In order to cool the DC motor and the driver board, which is fixed to the aluminium housing with copious amounts of thermal paste, the suction side of the compressor flows through the housing and motor. On top of the driver board sits a controller that knows how the turn the motor in the right direction and provides a soft start by ramping up from 0 to the desired RPM. This controller takes it's input from either a 3 setting lead (4 wires) which allows you to select 2000/3500/5000 rpm or takes a 400h PWM signal where 5% duty cycle is 2000 RPM, 65% duty cycle is 3500 RPM and 95% duty cycle is 5000 RPM. The version you order does not matter since the internal connector is the same and you can simply switch the lead from one to the other. I have not yet tested PWM. In any case, it is the lower driver board that contains a bunch of beefy FET's that failed and I tried to see if I could either repair it, remake another version of get some spares.
Suffice it to say that our chineese friends are not in the habit of producing anything that is even close to durable so spare parts were of course never thought of. You are supposed to consume product and buy more when something breaks. This has put of me off of these units but after some soul searching I had to come to the conclusion that I am already invested in this solution and I had to push on with it. So, I ordered another complete compressor thinking that at least I had a spare one when the mechanicals would wear out.
Now that I had a working compressor I checked my dodgy test wiring at least 5 times to not burn out another unit and.. it started spinning :) Once I had that all set up I mounted a relais between the original compressor clutch power connector and ground and wired the 12v unit up so that it would switch the high setting. After triple testing that everything worked as it should I drove to my local A/C shop to make an appointment for some custom work. Yesterday I finally got to get the entire system plumbed up and it was a good day of working alongside the experts. Really nice blokes who got my idea and simply allowed me to work along side them in their workshop. I did all the "range rover specific" stuff, or should that be "my handywork" :) and they were there to help with the A/C specific stuff. In the end we removed the flexible hoses that run to the original compressor from the aluminium pipes and replaced them with new ones and some angled fittings that were then routed to the new compressor. All in all not that much material was needed to get that done since the original plumbing already routed through that area, but still half a days work.
Then came the BIG moment! filling up the system and checking if it works. Originally the P38 contains 1250 grams of r134. The guy at the shop figured since we altered the plumbing and removed the original compressor which has a large internal volume that we should reduce that to 900 grams and take it from there. I fired up the engine, turned the HEVAC to "LO" and full blast and waited to see what happens. To my relief the "little compressor that could" was capable of running in a system that was designed for a much bigger capacity compressor! The suction line got nice and cold, the air blowing out the vents was freezing and the cycling (because the evaporator would freeze or any other reason the HEVAC computer would toggle the clutch) worked as well, though not as the belt driven unit would behave.
When we tested the system at around 20c we got 2 bar (130 psi) low side and 9 bar (130 psi) high side which is about right. I took the car for a drive with an eye on the current measurements from my victron shunt and I must say, the A/C worked well. Of course we still need to have a 30C + day which we will have next week so that should be interesting. The total current drawn by the vehicle never got much over 110A (and I know the car uses around 30 when just running) but at idle (in drive at the stop lights) the voltage would drop to around 12.5v so clearly the alternator that I currently run is not able to keep up at such low RPM's and the battery cops a beating for a few seconds.
The one thing I did observe is that the ramp-up of the compressor is quite slow and the HEVAC does not understand this, that is to say it is not designed for that. So when the compressor is disengaged, it does not ramp down slowly, it just stops. But when the A/C request line is brought up high again in stead of the evaporator immediately cooling down again it slowly cools down and since the blowers did not slow down you can feel the humidity from the evaporator entering the cabin just briefly. Suffice it to say that my own climate control algorithm will have to take that into account. Perhaps I will simply run the compressor speed up/down as required to keep the evaporator in equilibrium.
What's next? Well I intend to test the pants of the system whilst my car is still in running condition, ie. before I start work on the other projects. Next week is probably the last week of 30+ temperatures in this neck of the woods so I also plan to play around with the A/C then. I will try the low and medium setting and see what that does and see how the entire thing will cope with a heat soaked car that has stood in the sun for quite some time etc. I reckon that it will be able to handle, just, but that is good enough since my build will remove a lot of windows, replacing them with insulated walls so there will be a larger area to cool, just not one that will have that much light incidence.
To be continued :)
Cheers,
-P