knp
16th June 2008, 07:52 PM
Gedday,
Back in September last year MrC hit 60,000km and with that we got a nice cracking sound from first the drivers window and then front passengers window. From what I've read in this forum it is a fairly common occurrence when you get to around this distance.
Anyway the problem turned out to be cracked plastic wheels on the window regulator in various stages of disintegration. A search of this site turned up a number off options to fix and all involved removing the regulator from the motor and either drilling/welding or doing stuff beyond my capabilities.
So this is a bit of a variation on an old theme since I'm a big fan of least is most and I also didn't trust myself to be able to re-fit and re-adjust the regulator again once I had it fixed.
This is what the old man and me came up with over a few too many whiskeys one night we hit upon the idea of a split bearing block to replace the roller. (We weren't binge drinking - just lubricating the grey matter - honest :D) Errrrupppp! - better have another one I 'spose...
So here are some pics. We went through a number of prototypes and ended up with a pretty accurate duplication of the original roller but in a square block slider form.
Start with a slab of 12mm thick nylon. Can be oil impregnated but not really necessary. Cut out a block 27mm x 40mm.
You then route out a 6mm rebate (refer to diagram below) along each side and drill an 8mm holes with a 12mm countersink 2mm deep in the middle. Then split into 2 halves with a 1mm tenon saw which should give result in a width of just under 26mm. Result is 2 halves that will fit together almost perfectly. Note: before sawing in half you can drill some screw holes so that the halves can be screwed together to enable easy drilling out of the hole. Then you re-drill the 8mm and 12mm centre holes as they will elongated after cutting in half.
To fit you remove the old roller and slide the channel out far enough to get the 2 bearing halves onto the regulator shaft. Then slide bearing back into channel and reinstall channel onto window.
This is the latest and greatest version with the screws. I only added the screws to make it easier to drill out the holes for the regulator shaft. The screws are not needed to hold the blocks together in service - the channel does that.
http://img515.imageshack.us/img515/5837/sany0007qf1.th.jpg (http://img515.imageshack.us/my.php?image=sany0007qf1.jpg)
http://img504.imageshack.us/img504/445/sany0006gg9.th.jpg (http://img504.imageshack.us/my.php?image=sany0006gg9.jpg)
http://img363.imageshack.us/img363/8086/sany0005ng1.th.jpg (http://img363.imageshack.us/my.php?image=sany0005ng1.jpg)
Rough diagram:
http://img401.imageshack.us/img401/6456/diag1rb7.th.jpg (http://img401.imageshack.us/my.php?image=diag1rb7.jpg)
You need to allow for the width of the saw cut when cutting the original size. e.g. my tenon saw makes about a 1.1mm cut so I set the width of 27mm and after cutting in half, end up with a block width of just under 26mm which works just great. The inside of the window channel measures 26mm.
This one shows two good-uns in the foreground (on the specially built router table), some rejects in the back and a failure on the right where the router bit me:
http://img403.imageshack.us/img403/1892/sany0056uy0.th.jpg (http://img403.imageshack.us/my.php?image=sany0056uy0.jpg)
This shows the new bearing block in place:
http://img84.imageshack.us/img84/4575/sany0051ow3.th.jpg (http://img84.imageshack.us/my.php?image=sany0051ow3.jpg)
Materials used: 1 old nylon chopping board - used for prototypes - too thin. 1 slab of oil impregnated nylon any size but has to 12mm thick to avoid too much sanding which is a pain. I also had some nickel anti-seize on hand and I used a dob of that for lubrication too.
The original piece of oil impregnated nylon came from the scraps in Dad's workshop but I have since found a good supply at Reverse Garbage here in Brisbane.
Please contact me if there's anything else I need to explain.
Cheers
Peter
Back in September last year MrC hit 60,000km and with that we got a nice cracking sound from first the drivers window and then front passengers window. From what I've read in this forum it is a fairly common occurrence when you get to around this distance.
Anyway the problem turned out to be cracked plastic wheels on the window regulator in various stages of disintegration. A search of this site turned up a number off options to fix and all involved removing the regulator from the motor and either drilling/welding or doing stuff beyond my capabilities.
So this is a bit of a variation on an old theme since I'm a big fan of least is most and I also didn't trust myself to be able to re-fit and re-adjust the regulator again once I had it fixed.
This is what the old man and me came up with over a few too many whiskeys one night we hit upon the idea of a split bearing block to replace the roller. (We weren't binge drinking - just lubricating the grey matter - honest :D) Errrrupppp! - better have another one I 'spose...
So here are some pics. We went through a number of prototypes and ended up with a pretty accurate duplication of the original roller but in a square block slider form.
Start with a slab of 12mm thick nylon. Can be oil impregnated but not really necessary. Cut out a block 27mm x 40mm.
You then route out a 6mm rebate (refer to diagram below) along each side and drill an 8mm holes with a 12mm countersink 2mm deep in the middle. Then split into 2 halves with a 1mm tenon saw which should give result in a width of just under 26mm. Result is 2 halves that will fit together almost perfectly. Note: before sawing in half you can drill some screw holes so that the halves can be screwed together to enable easy drilling out of the hole. Then you re-drill the 8mm and 12mm centre holes as they will elongated after cutting in half.
To fit you remove the old roller and slide the channel out far enough to get the 2 bearing halves onto the regulator shaft. Then slide bearing back into channel and reinstall channel onto window.
This is the latest and greatest version with the screws. I only added the screws to make it easier to drill out the holes for the regulator shaft. The screws are not needed to hold the blocks together in service - the channel does that.
http://img515.imageshack.us/img515/5837/sany0007qf1.th.jpg (http://img515.imageshack.us/my.php?image=sany0007qf1.jpg)
http://img504.imageshack.us/img504/445/sany0006gg9.th.jpg (http://img504.imageshack.us/my.php?image=sany0006gg9.jpg)
http://img363.imageshack.us/img363/8086/sany0005ng1.th.jpg (http://img363.imageshack.us/my.php?image=sany0005ng1.jpg)
Rough diagram:
http://img401.imageshack.us/img401/6456/diag1rb7.th.jpg (http://img401.imageshack.us/my.php?image=diag1rb7.jpg)
You need to allow for the width of the saw cut when cutting the original size. e.g. my tenon saw makes about a 1.1mm cut so I set the width of 27mm and after cutting in half, end up with a block width of just under 26mm which works just great. The inside of the window channel measures 26mm.
This one shows two good-uns in the foreground (on the specially built router table), some rejects in the back and a failure on the right where the router bit me:
http://img403.imageshack.us/img403/1892/sany0056uy0.th.jpg (http://img403.imageshack.us/my.php?image=sany0056uy0.jpg)
This shows the new bearing block in place:
http://img84.imageshack.us/img84/4575/sany0051ow3.th.jpg (http://img84.imageshack.us/my.php?image=sany0051ow3.jpg)
Materials used: 1 old nylon chopping board - used for prototypes - too thin. 1 slab of oil impregnated nylon any size but has to 12mm thick to avoid too much sanding which is a pain. I also had some nickel anti-seize on hand and I used a dob of that for lubrication too.
The original piece of oil impregnated nylon came from the scraps in Dad's workshop but I have since found a good supply at Reverse Garbage here in Brisbane.
Please contact me if there's anything else I need to explain.
Cheers
Peter