Yes the followers and every thing was removed to do the machining of the head.
I was a bit misleading about it running so well . Everything is a bit relative when it has not been running for a week.
I took it to be going well. However when it was taken into heavy traffic in the city it did show it's faults.
Main reason for the gasket change was pressurization of the coolant it ran like a clock before that.
Thank you both for your help. I will have a go at it tomorrow.
I have not been locking the crank in the bell housing. It is auto. What do I lock is with? I don't see why I have to lock it if the cam is not moving . What am I not seeing?
Also I note that when the detent in the cam is in line with the pin hole on top that the cam is not anywhere near the highest point of the cam lobe.Is this wrong?
No, no silicone in the halfs.

