I've done 4 plugs. One came out easily, it had nicker anti-seize on it. The other three had to be worked out, I sprayed WD40 down the hole after loosening the plugs a little and let it sit for about 30 minutes or so. That help enormously.
I got an old plug and ground off the electrodes. I then ground a groove up the side of the threaded section to make a thread chaser. I wound that in with a bit of rubber tubing over the insulator. It wound in easily and brought out a minimum of gunk (I had smeared a littel grease into the groove to cat any gunk.
Despite what the NGK site says, I've smeared the new plug threads with nickel anti-seize. The workshop manuals says 23 ft lbs for the torque wrench. However, I reduced the setting on the wrench to 20 ft.lbs to allow for the lubricant effect of the anti-seize and it still seemed more than I would normally apply. In fact, I didn't let the wrench click off (it's a Warren & Brown 3/8" deflecting beam unit used on my motorbikes).
326__19924.1471151766.jpg
Before all this started I had a persistent misfire on no. 4 cylinder (according to Faultmate).
Today, when I pulled out the coil (coil on plug design) a very fine length of copper wire, about 100m long, came out with the coil assy. It was along the plug boot. I wonder........
Bookmarks