Originally Posted by 
Wilbur
				 
			Hi Pat,
 
In my case, I presume the jet fitted was too large for the pressure differential between the gas pressure and the manifold pressure. This is why it over-gassed. The installer just fitted the jet size specified by D-gas, and didn't test it properly. My car is pretty noisy and I didn't hear the extra noise - I went out and covered 400 k's as suggested by D-gas to test the gas ratio usage which turned out to be over 40%.
 
I don't know what is actually causing the extra oil usage. It has been suggested that the extra heat of detonation damaged the rings. It has always worked hard since I have had it, but only started using oil after I covered the 400 k's of testing with D-gas.
 
However, there may have been some other problem with my installation because other than increased noise, there was absolutely no change in performance and very minimal or no reduction in diesel fuel usage.
 
I am glad your system is working - I wish I knew the difference between your set up and mine!
 
Cheers,
 
Paul