I managed to get quite a lot pf work done on Wilf over the weekend. Replaced the clutch slave cylinder and the clutch and gears are working fine. Even managed to take him for a short drive with a seat tied to the chassis! Went through the transmission and all gears and all worked fine. Even the brakes kind of worked with a LOT of pumping. That will be the last drive for a long time.
I got all the dash panels out and got all the electrics that were inside the cabin through to the engine bay - I am dreading when it comes to getting all those wires reconnected.
I flushed the radiator and engine and then removed the front panel and radiator. I found the panel was rusted through - looks like a difficult repair.
I also noticed a lot of silicon around the section where the head hose goes into the engine. Looks like someone has tried to stop a leak.
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