Series II engine strip down
well half an hour presented itself this afternoon so i managed to get the head off and get a bit of a look at was left of the bores etc etc
head gasket was composite and intact with no traces of cylinder leakage...
only got to clean up the top of one bore in the time i had
it's had a hard life it would seem.... but certainly not the worst i have seen it has to be said....
pics to follow....https://www.aulro.com/afvb/images/im...017/08/722.jpg
https://www.aulro.com/afvb/images/im...017/08/723.jpg
full of years of squirts of oil and other crud thats made its way into the pots..
https://www.aulro.com/afvb/images/im...017/08/724.jpg
a pic showing the water pump location on the block. it is about 1.5" lower than the later blocks from memory...
https://www.aulro.com/afvb/images/im...017/08/725.jpg
a couple of lips that aint for kissing.....
https://www.aulro.com/afvb/images/im...017/08/726.jpg
A 3 stamped on the piston. it is pot 3, so i imagine the A is for the fitting tolerance. no oversize stamping but i have to go looky see how they are normally marked as i dont positively recall what it is.
yep A stands for .0002" to .0004" above nominal size...
and the bore measures up as standard 3.562" using my old verniers.