Ok, lets update this.
The head was built, with almost all new parts, refitted, still smoked.
Compression test revealed very low results. in the range of 150-165psi.
Not good so I have pulled it out - few pics for anyone keen to see how it progresses.. I will do a proper thread on how to rebuild it when I find out how to do it!
Removing the engine. I removed the head seperately as I managed to round one of the belhousing bolts
https://www.aulro.com/afvb/images/im...11/12/1261.jpg
Clutch and flywheel removed. Some evidence of heat/slipping on it, and there is a reasonable amount of play on the flywheel, more worryingly play like a wheel bearing as opposed to rotational freedom.
A solid flywheel from Rakeway will go back in the same as my 90.
https://www.aulro.com/afvb/images/im...011/09/948.jpg
Removing the ancillaries:
https://www.aulro.com/afvb/images/im...011/09/949.jpg
https://www.aulro.com/afvb/images/im...011/09/950.jpg
Remove oil pump:
https://www.aulro.com/afvb/images/im...011/09/951.jpg
One bolt was missing and is broken in the main bearing cap:
https://www.aulro.com/afvb/images/im...011/09/952.jpg
Next remove the front pulley. This is ridiculously tight. 340lb/ft I think I made a tool, then ratchet strapped the whole lot to the bench, and got someone to stand on the end of the tool while I also stood on it an undid the bolt. (thanks to the JC technical support line to check the thread direction!:)):
https://www.aulro.com/afvb/images/im...011/09/953.jpg
Crank looks good:
https://www.aulro.com/afvb/images/im...011/09/954.jpg
Main bearings all look good, but 3 of the 5 big end bearings on the rod side are through the white metal.
https://www.aulro.com/afvb/images/im...011/09/955.jpg
The bores look ok, as do the pistons, but they are obviously slightly dodgy!
Will grab some pics of those in day light tommorow
Crank looks perfect.

