Originally Posted by
Ralph1Malph
Still in the process of obtaining another MAF, however....
I decided to bypass the wastegate modulator and I believe it is faulty as well. The attached file is a longer flatter run with the modulator bypassed and MAF disconnected. I would say that it is running as well as I have ever had it run. Of course there was not much load but the signs are encouraging as it did not surge or overboost once.
However, when I took the air intake hose off my mood changed.:( There was sandy grit coating the inside walls of the intake hose.:( (Makes sense as the filter had blown through and we have done sand driving).
A quick look at the turbo intake vanes and some slight grittiness around the throat there too!:mad:
Worst of all, I detected a slight but definate movement of the shaft when I tried to wobble it with my fingers. Enough movement to actually concern me.:thumbsdown:
So, the list now includes a MAF (was replaced in 2010), wastegate modulator and maybe (price permitting) a turbo charger.
Reckon I should look at a snorkle as well to keep the intake above water and sand.
Grrr.
Cheers
Ralph