Yeah, I thought of that - and I'm sure that its a factor, but I reckon if I sneezed on the steering wheel I could pull a 180 :D I assumed that the 4BD1 pump was pushing more fluid through or something.
No smoke issues second time round, so I'm guessing it was overfuelled because the turbo wasn't set up correctly first time.
Learned that if you take out the fuel screw you can do wheelspins :D And blow off silicon elbows :D

