Ill have to learn how to do that annealing trick one day.
well a definite improvemnet. feels pretty much like normal, maybe a little better than pre Friday's event. I would put that down to excessive play between the actuator rod fitting and the external plate. EGTS are much closer to normal with only getting up to 250c Post/T on a hard excelleration up to 80km/h through the gears and in to 4th, with it starting to fall a little when leveled out 80km/h. The more destinctive turbo whistle has now gone back to normal as well. This was only a 2-3km short run. I will do some more with inspections today.
nothing seems to be leaking at this stage. I will keep an eye on that banjo fitting. The turbo to manifold did not have a gasket??? and as for the 3 studs/nuts, well if it wasnt for my beautiful Snap-on Hi-po 0 offset ring spanner, I think I would still be trying to get those undone. Torque was set at FT!
the hardest thing for me doing this, was self-doubt. Not having the "feel" for certain things like bolt tightness etc...and it is always hard to tell when getting in for that first drive as being a bit worried, emotion comes into play and the senses are hightend, which is hard to remove that from logical judgment of the small things
thanks to all that chipped in a helped. Especially Rick for putting up with my phone calls

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