Maybe not dead, but certainly severely poorly. Presume it's a 3.9, not 3.5?
If you're loosing coolant, and have low compression, then it's possible you have dead head gaskets, or dropped liner(s).
How much coolant does it use? Does your coolant header tank pressurise and overfill?
Does it have a good Service history?


. Went searching for pcv valve but cant find one????? This morning tried again, went for a drive and all seemed good, that was until the thermostat opened and the temp gauge was showing operating temp then it was driving at a snail pace and running on 5 or 6 again with a couple of back fires thrown in for good measure. So rang a landie knowledgeable mechanic in Adelaide and was told by sounds of it could be a dead engine. Have done a compression test. Results 1. 150psi 2. 135psi 3. 130psi 4.100psi 5. 135psi 6. 110psi 7. 145psi 8. 120psi. Not the best but Ive had old holdens running for years on similar numbers. It is losing a little coolant but the lower radiator hose has a slight leak and needs replacing. Anyone have any advice or theories as to why it is running so bad at operating temp. It ran perfectly from Adelaide to whyalla when i purchased it and sat for a week while I soaked the breather then all of a sudden this
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. Ahh being all alloy they have a liner for the bore.... are they prone to shifting?? Bit worried bout the low compression on two middle cylinders....head warp??? or blown gasket. Strange how it just happened all of a sudden though
. The T piece I need to check as I am unsure if it is the original one. Small amount of carbon to throttle body stub not enough to worry about though I dont think. Yeah it was the oil separator that was cleaned out. Pulled the mesh out and soaked in degreaser cleaned the body out let it all dry reassembled and reattached. Nothing else was disturbed but I have now since doing compression check removed and replaced the maf to throttle body and made sure connections are good. It seems like once warm enough and under load this misfire is happening. Im not sure if the heads have been removed previously and the rocker cover gaskets were done just before I purchased the vehicle so I havent removed anything electrical.......Yet. The old girl is a july 96 model with 242000 on the clock. Thought it might have had quite a few more good kms left in it yet. Everything when I bought it was spotless, was detailed beautifully even an engine bay steam clean so no signs that I could spot of previous leaks and such.
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