Yeah right - are you going to catch the train to get here?
![]()
"How long since you've visited The Good Oil?"
'93 V8 Rossi
'97 to '07. sold.![]()
'01 V8 D2
'06 to 10. written off.
'03 4.6 V8 HSE D2a with Tornado ECM
'10 to '21
'16.5 RRS SDV8
'21 to Infinity and Beyond!
1988 Isuzu Bus. V10 15L NA Diesel
Home is where you park it..
[IMG][/IMG]
Yeah right - are you going to catch the train to get here?
![]()
Scott
not at the moment,,![]()
"How long since you've visited The Good Oil?"
'93 V8 Rossi
'97 to '07. sold.![]()
'01 V8 D2
'06 to 10. written off.
'03 4.6 V8 HSE D2a with Tornado ECM
'10 to '21
'16.5 RRS SDV8
'21 to Infinity and Beyond!
1988 Isuzu Bus. V10 15L NA Diesel
Home is where you park it..
[IMG][/IMG]
Well it seems there is an issue, plugs from #1 and #7 came out of the engine wet
Hoping it's only a head gasket !
Steve
Fingers crossed for you Steve!
Gary
2007 Range Rover Sport TDV8
Modified 1996 p38a HSE sold
It also looks very much like there has been oil seeping out under the heads as well
Should have them off in the next couple of hours !
Steve
Take pics of everything,,
only because in 6 months time you'll be saying "Why didnt I---"![]()
"How long since you've visited The Good Oil?"
'93 V8 Rossi
'97 to '07. sold.![]()
'01 V8 D2
'06 to 10. written off.
'03 4.6 V8 HSE D2a with Tornado ECM
'10 to '21
'16.5 RRS SDV8
'21 to Infinity and Beyond!
1988 Isuzu Bus. V10 15L NA Diesel
Home is where you park it..
[IMG][/IMG]
Well the heads are off and I suspect the main problem was those stretch bolts. On this motor the head bolts felt very loose, i could have undone most of them with a ratchet ! I remember on the original motor we had the long bar and had to bust a gut to loosen the head bolts.
No 7 piston has been getting steam cleaned and there is a surprising amount of buildup of crud in the upper areas of the engine. I think i will use flushing oil in it when I reassemble the motor.
Apart from that it all looks pretty good, no wear on the rocker arms or cam so it should go back together nicely.
Getting the heads crack tested and checked tomorrow
Steve
Steve, that's exactly how my cyls were. Blew both gaskets through to the water port. A number of my head bolts were also loose.
I ended up getting both heads surfaced even though they were mostly within spec and used the payen brand bolts and Elring gaskets. I sold the engine because of my Ford V8 conversion but if I kept it, ARP studs for sure!!
I've heard that loose head bolts are not a cause of a blown head gasket but the result so I don't think they're anything to actually worry about.
Scott
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