Originally Posted by
Blknight.aus
press straightened after cooking warped it, shaved extensively and not re-hardened In the areas where it hadnt been scoured there was evidence of some of the worst machining I've ever seen on an engine component, Without exagerating I could have quite probably done a better job with a set of long hand files
It's second failure method was either melting of the head between the 2,3,+4 pots or massive head rewarping allowing the hot gasses to do the damage after the gasket failed.
it was bad enough that the cam journal and face were visible distorted.