Well, look on the bright side... you at least have a project now :) That is... if you were running out of them to begin with :D
Printable View
Well, look on the bright side... you at least have a project now :) That is... if you were running out of them to begin with :D
Well transfercase is back together and ready to roll.
Gearbox should be done tomorrow.
With everything apart i also noticed the clutch fork was stuffed and the thrust bearing is on its way out too.
Will pull the clutch while i have it all apart and see how that looks too.
Its alive at last!!!!
Was up and running Monday and so far so good:)
Here's what i replaced
Output Shaft $350.00
Transfer Case Input Gear $250.00
Thrust Bearing $65.00
Clutch Fork $75.00
Various Seals $15.00
Oil $25.00
Just want to say a big thanks to everyone for there help,offers of help and advice:)
Great to hear mate ,Hope you have a good trouble free run for now on:D
defenderkev,
was the input gear to the TC cross drilled? I understand that this was the mod to improve lubrication to the splines. I had the splines on the GB output shaft and TC input gear go. It was the first time that I found out that this was a common problem. Bloody LR, they should have put out a recall or at least a service bulletin.