Thanks Dave.
I ended up just flushing about 4L of clean fluid through the cooler with the hoses still connected. Had some clear hose on the outlet so I could see what it looked like. Definitely very yuk to start with but cleared up after a couple of liters.
Picked up the torque converter on Saturday. Apparently they had to source a replacement top half for it as it was broken internally. The guy that was there when I picked it up wasn’t the one who did it so couldn’t give me any more info.
Transmission is back in the car now and transfer case refitted.
Transfer still needs an overhaul and the case sleeved but that’s a job for ‘Ron.
All going well I’ll know by the weekend whether my first auto rebuild has been a success or not.
Fingers crossed!
Steve
1985 County - Isuzu 4bd1 with HX30W turbo, LT95, 255/85-16 KM2's
1988 120 with rust and potential
1999 300tdi 130 single cab - "stock as bro"
2003 D2a Td5 - the boss's daily drive
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