So, a properly working dizzy cap has made a great difference, as you’d expect. Changed plugs, cap and rotor button. Plugs all looked fine and even but a bit black which confirmed my thoughts it was running rich (you could smell it too).
Checked static timing - a bit of a pain with an electronic module as you don’t get the spark a set of points gives you when doing this, but a faint click can be heard - set it to about 9 degrees BTDC - it was very close to this anyway. Spec is 8 degrees for the low compression engines and 10 for the USA spec high comp engines, so split the difference. 👍
Once these things were all done, killed 2 birds with one stone and pulled the rocker covers to fix slight leaks, and to check tapped clearance (even though I wasn’t go as far as to fix any that were out). Found only one out of spec - number 2 inlet is a tad wide at 0.4mm (spec is 0.3 to 0.35) so that’s probably the one I can hear. PITA of a job to re shim it, so I’ll let it go for now, all the others were in spec soma good clean of the mating surfaces, some hylomar on the new gaskets and hopefully that will keep the leaks at bay from the top end for a week or two... 😉
Pulled the air cleaner assembly off so I could tune the carbs now I was happy with everything else. Front carb was waaaaaaaaay out of whack - blind and deaf Freddy could have heard it. Balanced them by ear and set the mixtures as best I could (will take it in for a proper tune at a place recommended soon) But I got the idle much smoother although not perfect - think I’ve got a small vacuum leak too but couldn’t track it down.
Back together with everything and took it for a test run - gave it a fair bit of stick to burn some oil off the exhaust manifold and to see how it went - and it goes very well. Probably a fraction more power than before but a lot smoother through the rev range and it seems to kick down to second a bit easier now - really had to sink the boot in before. Maybe I’m imagining it, but it ran a bit cooler too - didn’t get it over the ‘N’ in ‘Normal’ which it hasn’t sat at before. Even gave the AC a blast but it was a beautiful ‘Windows Down’ afternoon yestereday - about 28 degrees, very comfortable motoring.
So, think I’m happy enough to take it on a long run this weekend - I’ll report back Sunday night to let you know how it went...


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real gentlemen car sure you will have many great sunday drives


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