If you know someone with a milling machine you could adapt a large socket.
Isuzu C240 powered Series 3
I've actually cut & extended it now to make it more user friendly.
One problem I found is that you can make it too accurate, problem is the aftermarket nuts are not as accurately made as the originals.......
Colin
'56 Series 1 with homemade welder
'65 Series IIa Dormobile
'70 SIIa GS
'76 SIII 88" (Isuzu C240)
'81 SIII FFR
'95 Defender Tanami
Motorcycles :-
Vincent Rapide, Panther M100, Norton BIG4, Electra & Navigator, Matchless G80C, Suzuki SV650
Well, I don't think this one is too accurate- but it fits.
It may not withstand 80 foot-pounds, so I'll probably hold back a bit from that. It's only mild steel pipe, so I'd better not load it up too much.
I may not have the paper gasket for the cover. Could I just use some thin card and cut one out and coat it with the appropriate brown goo?
Cheers
Coop
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you dont need a top notch socket. almost any cheap deep reach impact socket will do the job.
if you're worried about it slide it inside a piece of pipe thats a snug fit. IF you get really clever you also taper the "fingers" that go into the holes so the ID side is the longest this gives you a tool that when you push it on and tap it home it plunges the locktab out of the way.
you will be quietly amazed at how tight you can get a castle style nut with a drift and hammer.
If the nut breaks the tabs of the locking washer you have a couple of issues the first is yes the nut is not tight enough but the second is that the splines are loose in the gear and allowing it to twist the washer, this is what starts the process of unwinding the nut and ripping the washer apart.
if you come across another one check the wear marks on the washer.
Dave
"In a Landrover the other vehicle is your crumple zone."
For spelling call Rogets, for mechanicing call me.
Fozzy, 2.25D SIII Ex DCA Ute
TdiautoManual d1 (gave it to the Mupion)
Archaeoptersix 1990 6x6 dual cab(This things staying)
If you've benefited from one or more of my posts please remember, your taxes paid for my skill sets, I'm just trying to make sure you get your monies worth.
If you think you're in front on the deal, pay it forwards.
Another problem I found was that the locktab was wider than the cutouts in the nut (pattern parts again!!) Worthwhile checking before you put the washer in place & tighten the nut.
Colin
'56 Series 1 with homemade welder
'65 Series IIa Dormobile
'70 SIIa GS
'76 SIII 88" (Isuzu C240)
'81 SIII FFR
'95 Defender Tanami
Motorcycles :-
Vincent Rapide, Panther M100, Norton BIG4, Electra & Navigator, Matchless G80C, Suzuki SV650
G'day all,
Good thread which has inspired me to make my own tool to fit the G/Box output shaft gear nut during the week. Took 1 1/2 hrs.
Found a 7/8" BS 3/4" Drive Socket and TIG welded a 1 1/8" AF 1/2" drive socket on the back or use a DEEP drive socket to clear the end of the main shaft.
Linished the end of socket square.
The inner teeth of the socket has to clear the bottom of the slots in the nut. (Had to ground about 0.5 mm off a few teeth.)
Clamp the nut on top of the socket.
Using a 0.4mm black felt pen mark the slot positions to create a black area.
Then using a 1mm Inox disc cut two grooves about 8 mm deep to match the nut slots.
Using a 6mm Inox disc grind down the area not black. Grind down about 8 mm.
Then it's trail and error to see which slot needs to be adjusted. This takes the time!!!.
I noted the nut slots are not exactly equal in size.
When it's right the nut will slid in easily at all positions not just one place.
A good thing about using the socket is the teeth are tapered inward so it also centres the socket on the nut. The end of the shaft slips nicely into the 3/4" drive square end. This give added support for the torque pull.
I always torque this nut to 105ft/lb.
15/05/2016. Just did a torque wrench pull test using a piece of 1/4" flat bar across two teeth only at 120ft/lb and it's still in one piece.!!!!amazing.
Hope this makes sense.
Chris
Well, the very rough socket I made from a lump of pipe got the job done. There was a tendency for the fingers to slip off the nut at maximum torque (as much as I could apply using about an 8" lever through the hole). Just to be sure it was tight enough, I finished it off with a hammer and drift, but I did not see the nut move any further when I did this. I doubt it was up to 80 ft-lb, but it got us to the northern Flinders and back again without making any expensive-sounding noises!
Cheers
Coop
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