Well yesterday, got the exhaust done....temporarily, very temp, so no pics
All seems well, just the fan wants moving back a little and its gutless
Got a scabby old Quadrajet and stuck the original 200impco of the side, the carb has holes everywhere and sticky butterflys
Got a recoed then pulled of for a holley, quady coming to work tomorrow for 100 beer tickets, then I can get some timing in it without raising the idle to much (because bytteflys wont clos) and set it up to run fuel before we head bush this weekend

,
troubles? well it wouldn't start without leaking vac, stop the leak and no go?? well it konked out pulling up with the 3.9 on gas, so just switched to fuel then yanked so didn't think into it, pulled the mixer apart and the little regulating bit on the diaphragm had dropped off

, stick it back together and all is well, everything except the tach is all good and no shakes/rattles/knocks, and thank god the auto works fine after dropping the pump off
So carby and low pressure pump in, tomorrow night after work, then I'll tune it wednesday before night shift and we're done

Bookmarks