Replaced all cooling system hoses [ except secret hose] , new radiator after old one failed the pressure test, cleaned intercooler with shellite, fixed power steering leak in low pressure hose [ new o'ring] ,removed drive belt & regreased idler pully bearings, checked H.B. , replaced missing bolt in coolant pipe system, took the time to scrub usually inaccessible part of engine bay with degreaser, treated the 4 bolt heads in the bottom of the battery box with kill rust after cleaning them, took for a test drive, held my breath..... ALL GOOD! so far Tomorrow I will get under & scrub all visible oil from the chassis with the intention of finding out if the power steering leak was the primary cause. This weekend I have a week of jobs for SWMBO to catch up on, no Bribie for the boys & I this weekend, Bob :p

